Experimental Study of Flight Effect on Fan Noise : 2nd, Report, Fan Noise Variations due to Flight Effect
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概要
- 論文の詳細を見る
Clarification of fan noise source variation due to a flight effect is important for a turbofan noise reduction and a noise estimation. A fan noise spectral extent and a range of fan operation influenced by the flight effect were studied experimentally using a large turbofan engine and a geodesic 4m diameter semi-sphere inflow control device that can simulate the flight effect on fan noise in static engine tests. The fan noise reduction by the flight effect in a fan approach condition was higher than that in a fan take-off condition, because the fan rotor generates BPF tones by itself near the take-off condition. The highest reduced component in fan noise spectra was a fundamental fan blade passing frequency (BPF) tone, whose reduced level was 20 dB at maximum. Higher harmonic BPF tones and a buzz saw noise were also reduced by the flight effect, but a reduction of broadband noise was not evaluated in the whole range of fan operation.
- 一般社団法人日本機械学会の論文
著者
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Morita Mitsuo
National Aerospace Laboratory
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KOBAYAHI Hiroshi
National Aerospace Laboratory
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TORISAKI Tadao
National Aerospace Laboratory
関連論文
- Aeroengine Research in National Aerospace Laboratory(Letters from R&D Groups)
- Experimental Study of Flight Effect on Fan Noise : 2nd, Report, Fan Noise Variations due to Flight Effect